All Work, No Play

We’ve been enjoying our stay with Donna’s parents near Old Bennington, Vermont. That’s not to say we haven’t had to handle a few projects – I’ll get to that in a moment. We’re parked on their property with a view of Mount Anthony from our door step.

View of Mount Anthony from our door step on the Connor’s property

Before we came here, I needed to replace our bank of four 6-volt house batteries. I ordered four Lifeline AGM batteries on Tuesday, June 5th, in Watkins Glen. I was told by the seller, Powerstride Sales, that I would have the batteries by the end of the week. Well, that didn’t happen and we had to change the shipping address to Donna’s parents’ house. I was told they would arrive there by Thursday, the 14th. At that time, I was in Binghamton fixing the overheating issue, so it didn’t really matter when they didn’t show up. I tracked them and they were in the Estes Distribution Center in nearby Glenmont, NY just outside of Albany. I figured they would be out for delivery on Friday.

When I arrived Friday night, they hadn’t showed up. On Saturday, I received an e-mail from Estes telling me that since the shipment was going to a residential address, they needed to set an appointment time to be sure I was there to receive it. It went on to say they would contact me in one or two business days to set the appointment! They were closed on the weekend, so I couldn’t do anything until Monday.

I rode the Spyder to Bennington Saturday and bought a brisket at Price Chopper. This grocery store had butchers in the meat department. I asked the butcher if he had a brisket flat that was about five pounds. He said he thought so and went into the back. A few minutes later, he came out and put a hunk of flat (HOF) on the scale – 4.97 lbs! How’s that for close to five pounds!

I set up the Traeger wood pellet fired smoker grill next to the garage. On Sunday morning at 5:30am, I had the HOF on the grill smoking. I smoked it for two hours before I raised the temperature setting to 200 degrees for the next four hours. I spritzed it with a spray bottle filled with a can of beer, two ounces of apple cider vinegar and two tablespoons of Worcestershire sauce every hour. When the internal temperature of the HOF held at 160 degrees, I wrapped it in foil and put it back on the grill.

A couple of hours later, it was at an internal temperature of 198 degrees so I took it off the grill. I left it tightly wrapped in the foil, wrapped two towels around it and stuffed it into the microwave oven. Keeping it insulated in a tightly confined space held the heat and the meat continued to cook as it slowly cooled. A few hours later it was ready to serve. It came out tender. I think it could have been juicier, but it was good.

Donna’s sister Linda and her husband Tommy came over. The six of us plus Tommy and Linda’s grandson Michael dined al fresco. It was great way to celebrate Father’s Day.

I know it looks like a charred piece of meat, but it’s tender smoked brisket hunk of flat

On Monday morning, I called Estes Freight. They had the batteries in Glenmont. I arranged to pick up the batteries there at 12:30pm. Tommy offered to drive me there in his truck to retrieve them. The woman I talked to said they would be ready at the loading dock.

When we arrived, I checked in at the dispatch desk. The guy told me it would take a few minutes and he told me where they would load the shipment. Tommy and I waited outside by the loading ramp. And waited. About 20 minutes later, a guy came out and said they had to move a trailer that the batteries were in, then he could bring them out on a forklift, but it would take a few more minutes before he could do that. Meanwhile Tommy and I watched the way they moved trailers around the distribution center with a specially equipped truck.

The truck was designed to quickly connect and disconnect from the trailers. It had a rear entry that allowed the driver to step out on the rear deck to connect the air lines. The coupler plate was hydraulically actuated so he could raise the front of the trailer, bringing the front jacks off the ground. Once he moved the trailer to the dock or wherever, he lowered the coupler plate until the trailer rested on the jacks and quickly disconnected and drove away to the next move.

Our wait of a few minutes turned into nearly 40 minutes, but the guy finally came out with 300 pounds of batteries on the forklift and gently lowered the skid into the back of Tommy’s truck and we were on our way.

I got started on the battery change around 2:30pm. First I had to pull the old wet cell lead-acid batteries. These are heavy.

Old battery bank – the house batteries are the ones with the black tops – the blue batteries are the chassis batteries for starting the motor

The new batteries weighed 66 pounds each. I took them off the shipping skid one at a time and then removed them from the shipping box and put them straight into the battery bay. Luckily, the new Lifeline batteries came with handles secured to the battery top with rope. This helped, but getting them into the bay involved bending over and extending my arms with the 66-pound load. Whew!

Lifeline AGM battery with lifting handles

The new batteries are AGM technology – advanced Absorbed Glass Mat. They don’t require any maintenance – no more adding distilled water and no more cleaning with baking soda as the acid accumulates on the batteries.

I also had ordered new 1/0 wire gauge foot-long cables with 5/16″ ring connectors to link the batteries. The bank is made up by wiring two batteries in series. This makes them into a 12-volt battery – it sums the voltage while the amp-hour rating remains at 220. With two sets of batteries wired in series, they are then joined in a parallel circuit. This keeps the voltage at 12-volts but it sums the amp-hour rating. Now I had a 12-volt battery bank with 440 amp-hours.

New battery bank

I was feverishly working to beat a thunderstorm that was coming. Once I had everything wired together, I double checked the connections. Then I went to start the generator to charge the batteries. No go. The generator wouldn’t crank and the start button LED began flashing. It would flash three times, then pause and flash three times again. Code three. There are three basic or first level codes. One flash means overheat. Two flashes means low oil pressure. Three flashes for all other faults – not much to go on there. By momentarily pressing the stop button, you can read the advanced or second level code. Now it flashed four times, paused and flashed six times. Code 46. This means low voltage at the generator.

I went back to the battery bank and started checking my connections again. By then the storm hit, but I was determined to solve the problem and got soaked over the next hour. Eventually I found that two ring connectors on the 2/0 gauge positive leads to the inverter and generator were corroded and had excessive voltage drop – I didn’t replace these longer cables when I changed the batteries. I figured removing the connectors from the old battery and installing them on the new had disturbed the internal bond between the cable and connector. I needed to cut the cable which is made of hundreds if not thousands of strands of copper covered with a heavy plastic insulator. Once I cut the cable back, I would expose clean copper and I could crimp a new ring connector on. The problem was, I didn’t have anything to cleanly cut the cable or crimp such a heavy connector. Now we were in worse shape than before – I couldn’t even run the generator!

2/0 ring connector – a quarter is in the photo for size comparison

On Tuesday morning, I went to Tractor Supply and bought an 18-inch bolt cutter, perfect for cutting the heavy cables. The bolt cutter also had a dimpled stop behind the pivot that I could use to crimp the ring connector. The heavy copper ring connectors were really stiff and hard to crimp. Once I had that done on the cables in question, the generator fired up and the Xantrex Freedom 458 inverter began charging the battery bank. I had to change the three-stage charging profile to match the AGM batteries. The Xantrex has four charging programs – one for standard wet cell batteries, two for gel type batteries and the fourth was for AGM. There are small differences in each charging profile that optimize the charge.

After a few hours, the batteries were good to go. We had good 12-volt power and the inverter was providing steady 120-volt AC power. I felt pretty good about it.

Later that evening, Donna and I were sitting the living room talking when we heard a whoosh and what sounded to me like ice cubes hitting the floor. It was water gushing from the fresh water supply to the toilet! I jumped up and shut down the water pump as Donna threw towels on the floor and began sopping the water up.

I found the water supply cut-off valve had failed. It’s a plastic 90-degree elbow with a quarter turn valve in it. The plastic separated at the valve and it blew apart! Well, now we had electricity but no water. I had a stiff drink and went to bed.

This morning, I rode the Spyder to Home Depot in Bennington and searched their PEX plumbing hardware. I couldn’t find the replacement shut-off valve, but I found a brass 90-degree elbow with 1/2″ PEX fittings on both ends. This would do. It was an easy fix and all is good now. PEX is really easy to work with.

We met up with Donna’s parents, Duke and Lorraine, and Tommy and Linda at TJ’s Fish Fry for lunch. We sat together and enjoyed the meal. Tomorrow we’ll pull out and continue our trek to Maine. I think we’ll make it to Cabela’s in Scarborough, Maine and spend the night there.

I’ll close this post with a picture of the front of the Father’s Day card from my mother-in-law, Lorraine.

 

One thought on “All Work, No Play

Comments are closed.