Our granddaughter, Lainey, is through with high school and also had the day off work on Thursday. After lunch on Thursday, we took some time to have a discussion on safe handling of firearms in preparation for a trip to the gun range. Back in the 90s, I was a certified Washington State Hunter Safety instructor. I also taught a class at Darrington High School on safe handling of firearms. The focus of the class was how to handle a firearm and also to recognize unsafe handling if you are ever in situation where someone is showing a gun.
After going through the safety lesson, we went to Norpoint Gun Range, about three miles from here. Lainey got to shoot a handgun for the first time. She found it much harder to shoot accurately than she imagined – it’s not like on TV! Donna also practiced and I had my share of rounds down range. Altogether we went through 250 rounds of ammo.
Lainey had fun learning to handle a gun. I think it’s an important skill to have. Anyone can can encounter firearms and if you don’t have a clue about how to safely handle or operate one, it can have tragic results.
There was another project I’d been putting off since we arrived here at my daughter Alana’s house in Arlington, Washington. The cord for the pull start on her lawn mower broke and needed to be replaced. I wasn’t putting it off so much as I was waiting for a day that wasn’t dark, dreary and raining. Working on the mower in a dark, cold garage wasn’t my preference – I was hoping for a sunny day to tackle the job in the driveway.
The weather took a turn for the better Thursday afternoon. I dove into the lawn mower repair. Replacing the pull-start cord seemed like a simple task at first glance. Well, as usual I had to start peeling the onion. First I took the plastic cover off the top of the Briggs and Stratton engine. Then I found the sheet metal housing for the starter pulley was riveted in place. I was hoping for sheet metal screw or bolts. I’m sure the rivets are used because it makes manufacturing simpler – no tapping threads for bolts and not enough clearance for screws.
Once I drilled out the rivets and had the starter pulley assembly in hand, I could see this may be challenging. I needed to wind the recoil mechanism of the starter pulley to tension it and then feed the pull-cord through two holes. Holding the assembly – which comprised the sheet metal housing, pulley and internal recoil spring – upside down in my hand, I didn’t pay enough attention to which way it was winding. It only provided sufficient spring tension in one direction, so I tensioned it and used a small punch tool to hold it in place while I installed the cord.
Sounds simple, but the cord was a little frayed and nearly impossible to pass through the two holes I needed to get it through. I tried cutting it clean and using a little super glue to stiffen it. No go. Then I used a length of safety wire and attached the wire with the thought of pulling the rope through. I got about halfway through then it was stuck. I had to use a small punch and hammer to get it through.
I temporarily attached the assembly with two rivets – instead of all four – to try it out. No go. The spring didn’t pull the start cord back – it was turning the pulley in the wrong direction. By then I was through. I figured it was best to attack it fresh on Friday morning. The weather forecast for the next several days is good.
On Friday morning, I got after the mower project again. I drilled out the rivets I’d installed the day before and went through the assembly steps again. This time I worked the recoil spring in the right direction, but it didn’t feel right. When I turned counter-clockwise as I should, it would provide some tension then it seemed to slip. In a clockwise direction, it increased tension with every turn. Puzzling to me. I managed to get the rope holes aligned with the peak tension in a counter-clockwise direction and went through the agonizing steps of threading the rope again. This time I got a little smarter and wrapped the frayed end of the rope with tape, then cut through the tape with a knife to make a clean, tight end.
I put it all together and installed two rivets to test it. No go. It wouldn’t reel in the pull-starter cord. There wasn’t sufficient tension. I took it all apart again. This time I went deeper and pulled the pulley assembly down to it’s component pieces. I found the problem. The spring inside the assembly was shot. Apparently when the pull-start cord broke, the pulley assembly rewound without any resistance and the spring was damaged. The spring is supposed to be a flat section of spring steel wound like a main spring on a mechanical watch. What I saw was a spring folded back on itself with random wavy areas.
I went to Arlington to the mower shop there – about two miles away. They didn’t have the part. They said they usually stock it and would have some on Tuesday. No good. We will leave on Monday and there’s no way Alana can reassemble what I took apart. The guy there told me the only other possibility was 20 miles away at The Shop in Mount Vernon.
I called The Shop in Mount Vernon, but only got voice mail. I took a chance and rode the Spyder up there. It was a beautiful day with the temperature in the 70s under blue skies. I went up SR9 to Lake McMurray, enjoying the sunshine and views all the way. This two-lane highway meanders through woods and the traffic was very light. From there I went west and up I-5 to Mount Vernon.
When I got to The Shop I found what I was looking for. They told me they try to always have this part on hand as it’s a common replacement.
I also bought five feet of cord thinking I shouldn’t be using the old cord to pull-start after this ordeal – after all it broke once and would likely break again sooner than a new one.
With all of the practice attempts at completing this repair, I had it back together in short order.
A pull test had the mower running in three pulls. It worked perfectly and retracted the pull-start cord as it should.
While I was working on the mower, I had another strange thing occur. In my last post, I ranted about Amazon not making good on a guaranteed delivery date. They offered me options for return and refund, but I thought it best to wait and see before I took up the offer for refund.
Friday morning I looked at the tracking info again and it showed out for delivery – scheduled for Monday June 26th. This didn’t make sense to me. If it was out for delivery, why wouldn’t it deliver that day? Well, the UPS guy showed up while I was working on the mower. He had two large boxes on a handcart and two smaller ones. I recognized one of the smaller ones as something I’d ordered, the other was for Alana. The two large boxes turned out to be an error as they were addressed to someone else.
He said, “Wait, I must have grabbed the wrong boxes, I show two more at this address.” He came back with the tires I ordered for Donna that were guaranteed to arrive Friday but showed they would arrive on Monday. Apparently it was a problem with the UPS tracking – the tires arrived on time.
Donna was out with Alana while I was working on the mower. They stopped at the computer repair place where the guy transferred the data from her hard drive to an external drive so she can easily set up a new laptop. Then they shopped at WinCo and Costco.
I grilled wild Alaskan sockeye salmon that Donna bought and we dined at the table in the front yard. Warm, sunny days are so much nicer than the weather we had last week!
We have another sunny day ahead and the temperature should reach the 80s. Donna and I plan to meet Sini for lunch in Edmonds. I need to start prepping the trailer for travel. We plan to pull out Monday and head over the North Cascade Highway to Winthrop for our next stop.
Mike, now you can add portable lawn mower repair and gun training to services you offer while on the road! Might make a few extra bucks to pay for diesel! 😉 Safe Travels! 🙂